January 15, 2019

Engulfment accident

A temporary worker was fatally injured after falling through a sugar hopper and becoming engulfed by sugar. The fatality occurred in a marine cargo warehouse operation, where bulk
granulated sugar from ships is transported to the warehouse for storage, bagging, and distribution. Sugar clumps often prevented the sugar from flowing freely through a hopper onto a conveyor
belt during bagging. Two or three times per shift, workers would manually break up the clumps. This fatal incident occurred when the temporary worker was breaking up sugar clumps with a pole/
shovel while standing on a hardened sugar bridge at the top of the hopper. The sugar bridge collapsed. As the worker fell to the bottom of the hopper, his legs went through the chute where
he was engulfed by sugar and suffocated.
SOURCE: OSHA

January 11, 2019

Fatal accident

Three employees were working on a leaking crude oil flow line that connected a production well to its tank battery. They dug a trench to access the leaking flow line and cut out a 6-ft. long section from the pipe using a cold cutter. Two of the employees attempted to thread the cut on the flow line with a manual pipe threading machine (threader) but the dies on the threader were dull. Therefore, the workers asked the office to have new dies for the machine delivered to the site. Instead of installing the new dies in the manual pipe threader that was used earlier, the dies were installed in an electric pipe threader. Two of the employees got in the trench with the electric pipe threader and started to thread the exposed pipe when flammable vapors were ignited by the electric pipe threader. As a result, a flash fire engulfed the trench in flames. The third employee discharged two fire extinguishers to extinguish the fire. The two employees that were in the trench were hospitalized with second and third-degree burns to their arms, neck and faces. One of these employees died at the hospital. The other burned employee was hospitalized and released at a later date.
SOURCE: OSHA

December 12, 2018

JR gestures | The Japan Times

JR gestures | The Japan Times: Dear Alice, Until recently I lived in Tokyo and commuted on the JR Chuo Sobu Line from Kameido Station. I made it a practice to ride in the last compartmen

December 8, 2018

Safety And Reliability: Two Sides Of The Same Coin

Safety And Reliability: Two Sides Of The Same Coin: Maintenance and reliability efforts are critically important in today’s industrial environment where increasingly complex and interdependent equipment are utilized.

December 3, 2018

Another Bhopal Anniversary.....

Time flies, but for the people who died a gruesome death on 2nd/3rd night, 1984, time was irrelevant. Today, we are in the cusp of technological innovations in process safety management, but the moot point is....can technology alone prevent disasters? Its people who make decisions, decisions that may compromise process safety and that could lead to a loss of containment incident. I am always of the view that technology can only be an enabler, if properly used.
There is a welcome change in India. Increasingly, boards of directors of chemical companies are focusing not only on occupational health and safety, but also on process safety. This is a welcome change. Lets pledge not to have another Bhopal again.

November 30, 2018

Choke clearing incident

A senior maintenance member of a two-man crew, and another employee were working from an elevated work platform. The platform was mounted on the back of a trailer, which was mounted to an asphalt tank. The employees had begun bypassing the normal asphalt storage tank to prepare for its five-year to seven-year cleaning. They placed a bypass valve in position to route the asphalt from the permanent tank to the temporary, trailer-mounted tank. Most of the asphalt piping was heated with a steam jacket encircling the pipes. However, the piping that ran from the bypass valve to the temporary tank was encircled with tubing that was heated by steam. The employees complained that the steam tubing, also referred to as steam tracing, was not wrapped tight enough, thereby preventing the pipe from getting hot enough to turn the hardened asphalt back to its liquid (melted) state. The employees then attempted to repair the clogged pipe. As was reported to be the normal practice, they went to the end of the asphalt piping outlet and began heating the last bend of the piping with a propane torch. The piping outlet was located directly over the top of the manhole opening of the heated asphalt tank. The tank was reported to be 300 degrees to 400 degrees Fahrenheit, at that time. During the site visit, approximately five hours later, the tank temperature gauge read approximately 260 degrees Fahrenheit. After an undetermined amount of time that the employees were using the propane torch to heat the piping, an explosion occurred in the asphalt tank. A witness described the explosion as a flame which shot 30 feet above the manhole cover and quickly descended back into the tank. This witness also stated that he could no longer observe the employees standing on the platform. Employee #1 remained on the platform and suffered asphalt burns and fractures to his face, where an item impacted it during the explosion. Employee #2 fell from the work platform, approximately 9 feet 5 inches to the concrete surface. Employee #2 suffered asphalt burns to his body and face, in addition to a hip fracture. A radio call for emergency response was broadcast throughout the company. The company Emergency Response Team doused the flames and provided initial first aid to Employees #1 and Employee #2. Both employees were transported to the hospital.
Source:OSHA

November 10, 2018

Minimizing Fire and Explosion Hazards in dusty systems

Minimizing Fire and Explosion Hazards in Dusty Systems: Having honest conversations about material handling hazards allow risks to be properly addressed, thereby reducing fire and explosion threats.

November 2, 2018

12 Tips for Centrifugal Pump Safety

12 Tips for Centrifugal Pump Safety: Centrifugal pumps are used in industrial settings, and there are several steps that should be followed to ensure safe and efficient pump operation.

October 29, 2018

On April 6, 1994, a unit operator was conducting rounds of the coker unit when he observed a leak coming from the mechanical seal of the heavy gas oil pump of coker unit #1. The operator decided to seek assistance; the head unit operator and six or seven unit operators responded. The operators placed water and steam on the leak to suppress the vapor from the seal. The head unit operator decided to shut down the pump and transfer the product to the secondary pump. As the operator shut down the primary pump, the mechanical seal blew, causing a vapor cloud to generate from the seal. The operators continued to put steam and water on the seal and isolated the pump from the pipe line. The remaining product in the pipe line leading to the primary heavy gas oil pump vaporized, leading to the dispersion of the vapor cloud. The operators who responded were wearing bunker gear and several wore emergency respirators. Those with respirators isolated the pump from the pipe line by closing the suction and discharge valves. The operators who were not wearing emergency respirators stationed themselves upwind of the vapor cloud and put water on the cloud; however, the wind changed direction several times, exposing unprotected operators to vapors. Employees #1 and #2, two unprotected operators who responded to incident, were brought to Hospital to be treated for inhalation of hydrocarbons. Employee #1 was hospitalized.
Source: OSHA

October 24, 2018

Hexane Vapors Ignited By Static Electricity; Worker Burned

Employee #1 was standing at the exit end of a conveyor, peeling off a build up of hexane adhesive from the inside of a stainless steel dip tank. A static discharge of electricity, apparently generated by the peeling action, caused a flash fire. Employee #1 suffered second degree burns on the back of his hands and his upper chest and neck. The tank is 12 inches by 15 inches by 22 inches in size. The employee was pulling adhesive from the back side of the tank when the fire started. All the equipment in the area is grounded and bonded and approved for the location. The flash point for hexane is -23 degrees.
Source:OSHA

September 18, 2018

Leak due to vibration

A specialized rubber manufacturing plant experienced leakage of a hexane solution from a pump discharge flange during use. The hexane vapor was ignited by a st atic electricity spark and a fire occurred. Apparently, the flange was loosened by vibrations from the pump.Routine operations were being carried out on site at the time of the accident.
The operation involved the transfer of a hexane solution from an un-reacted raw material recovery tank to the washing process through the outlet of the first flange of the pump. The hexane solution
leaked, ignited, and burned. The financial costs of recovery and lost production were significant.
Causes
The cause of the accident was a loose flange that resulted in leakage of a flammable substance. During the operation, a previously undetected cavitation in the pump produced significant vibration
which loosened the flange. As a cause of the ignition it was considered that the hexane was charged when it spouted from the flange, and static electricity was discharged; then hexane vapor ignited
and a fire occurred.
It was considered that the vibration might have been intensified by the passage of an insoluble polymer lump through the pump, a malformation in the substance generated on the piping wall. In addition, a reducer connected a 3-inch (~75mm) flange of the discharge pump to 6-inch (~150mm) piping. The looseness of this flange might have been accelerated when the force
of vibration was added on the piping.
Lessons learned
Vibrating equipment can increase potential for stress fractures and gaps from loosely fitting interfaces, all of which can be sources of leaks that, if undetected, may result in an accident. It is necessary to pay sufficient attention to vibrating equipment, especially pumps that may be found in many processes throughout the site. Control measures to mitigate potential risks could include regularly scheduled inspections in line with existing technical standards or in-house experience, particular attention to small-bore piping (vulnerable to fatigue), installation of a  vibration monitor to detect and locate abnormal vibration patterns, as well as other measures available in guidance
on vibrations from numerous sources.
Source: European Commission

September 14, 2018

Common Causes of Gasket Failure

Common Causes of Gasket Failure: During the course of our 50 years in business, Associated Gaskets has seen many different types of gasket failures. Sometimes these were seen late at night when we were called out to help with an emergency, other times it was when one of our own gaskets was returned after failing …

September 6, 2018

Global warming and its effect on process incidents

As the effects of global warming are being felt, chemical industries must acknowledge the fact for planning for natural disasters. The "Fire from ice" video about the Valero refinery incident and The Arkema incident due to Hurricane Harvey are two examples related to climate. Cyclone maximum wind speeds are increasing and past weather data may not be a reliable predictor about the future. What are you doing about it?

September 3, 2018

Gasket failure incident

On 5th January 2008 a production operator discovered a fair sized phenol leak in the phenol pump house next to the phenol storage tank. One of the gaskets on the flange connection on the outlet pipe of the tank had failed. The head of the operations department tried to stop the leak by tying a rubber belt around the flange. In the meantime, an operator sprayed water on the flange to avoid contact with phenol as much as possible. The phenol that had leaked was collected in a catchment pit of 20 m3 underneath the pump house. This catchment pit had a high level alarm, but it was not functioning at the time of the leak. The company was not aware of the malfunction because the alarm was not subject to periodic inspection.
An attempt was made to close the only manual valve on the pipe,located between the inner and the outer tank shells, but the valve spindle broke off during this manipulation, so the line could not be
shut off. After the temporary repair of the flange connection, three leaks continued to release phenol, which were also collected in the catchment tank. It was not allowed for the employees to enter the
pump house while the phenol was leaking. To clean up the catchment pit, the company provided a waste tank big enough to contain all the leaked phenol. When starting to pump the phenol from the catchment tank to the waste tank, it was discovered that the catchment pit had overflowed. Part of the
phenol/water mixture had passed over the rim of the open pit into the municipal sewer system. At the time, it was not yet known how much phenol had leaked to the sewer system.
On 7th January 2008 it was decided to start up the phenol-based batch production to consume all phenol in the storage tank since the phenol tank had to be taken out of service in order to replace
the gasket on the flange. On January 8th, after a few batch productions, it was found out that the level indicator in the phenol storage tank had become stuck since the last control of the level on 4th January (comparison of manual level measurement with level indicator). Only at that moment did the company realize that 25t of phenol had leaked out of the tank. The catchment pit probably
collected most of the release, but more than 5t of the phenol spilled into the municipal sewer. No consequences were reported as a result of the release into the municipal sewer. A specialized
company was hired to repair the remaining phenol leak.
Causes
In this case, a variety of causes contributed to the accident. The direct cause was the degradation of gasket that caused the leak. After the flanges and valves were replaced following the accident, it
was discovered that the valve broke down because the gasket next to it had been reacting with phenol over the course of many years, leading to a solid deformation that prevented the valve from moving,
hence, the valve could not be closed. The spindle of the manual valve at the tank broke off as a result of the deformation of the adjacent gaskets.
Source: European commission