May 29, 2020

Employee injured by exploding pump

Employee #1, the derrick man on a land oil drilling rig, was operating an auxiliary mud pump during the rigging-up phase of drilling in order to operate the cellar jet. The jet became clogged with rocks and debris, and the pressure relief valve on the pump did not operate. The high-pressure header on the pump came apart, and pieces of it struck employee #1 in the head. The pressure relief valve was found to have been set with a nail instead of a manufacturer's specified shear pin. The nail and valve had both corroded, rendering the valve inoperable. The high-pressure header was found to have suffered erosion around a fitting, which failed under pressure. No routine maintenance or inspection of the pump was conducted by the company.
Source:OSHA.GOV

May 22, 2020

Incident due to wrong catalyst added

At approximately 4:00 p.m. on February 22, 1998, Employee #3, a chemical operator, added the wrong catalyst for a reaction, causing overpressurization of the vessel. The safety relief valve opened, releasing vapors and liquid that settled to the ground near a roll-up door. Employees #4 through #12, contractors doing pipe fitting work on an adjacent reactor, were exposed to the vapors as they left the area. Employee #1 was exposed during clean-up and Employee #2 was performing housekeeping duties near the roll-up doors. Employees #1 through #12 were transported to the hospital complaining of nausea, dizziness, and chest tightness--all symptoms of acute chemical exposure.
SOURCE:OSHA.GOV

May 18, 2020

Breathing air hose crimp rings failure

At approximately 14.00 hours on 5th September 1988, an air supply hose on the discharge side of a portable breathing air receiver became detached whilst in use.One individual was carrying out an internal inspection of the Solvent Recovery Column at the time. He was therefore immediately deprived of an air supply.Very prompt action by the compressor attendant, with the assistance of a fireman enabled restoration of the air supply within a few seconds. An emergency call was made to the Fire Station for additional backup, but the individual concerned was able to make his own way out of the column, and suffered no physical effects.On examination the crimping rings attaching the pressure hose to the bayonet connection were found to be loose and showed no signs of ever being compressed.Following the incident, all work involving mobile breathing air systems was stopped. It turned out that all hoses arrived in vacuum sealed packs which were only opened at the work-site. No inspection or testing was therefore performed and no documentation accompanied the hose to indicate what Quality Assurance procedures had been followed.
Lessons
All hoses were examined and certified on site immediately.Some hose lengths were found to have only one crimp-ring applied, rather than the usual two. Initially it was accepted that a second ring should be applied. However, the contractor subsequently discussed this matter with the supplier who advised against this course of action. Clamping is normally carried out whilst the hose is being heat-shrunk onto the fitting. Any attempt to add a second clamp 'cold' might affect the integrity of the original bond.All such hoses were therefore withdrawn from service, and have been replaced by others, which incorporate an improved coupling design.For vessel entry the statutory requirement is for an outside observer who is similarly clothed (and therefore has breathing apparatus (BA) at the ready) whose primary responsibility is to summon assistance in the event of a dangerous situation arising, and to then attempt a rescue. The shutdown arrangements require each party to make its own arrangements for observers. This could therefore involve personnel who had only limited BA training. This situation was revised.
Source:ICHEME

May 14, 2020

Inadvertent mixing of chemicals causes fatalities



The accident occurred in a plant making dyes and a chromate dip for electroplated products. These products were treated in a series of open-topped tanks located in a sub-basement, known as the zinc-plating room, which contained two parallel rows of tanks separated by a grated walkway. A concrete drainage pit lay beneath the walkway. Ventilation in the zinc-plating room was provided by two ceiling exhaust fans, five windows and the door to the room were closed at the time of the accident.The last tank in the series, where the accident occurred, was used for drying parts after they had been electroplated. The tank measured 1.5 x 1.2 x 1.5 metres. The parts were suspended above the tank, and excess zinc cyanide solution dripped into the tank. Waste zinc cyanide was pumped from the tank once each year.On the day before the accident, an industrial cleaning and hauling company pumped the waste from the tank, leaving a layer of zinc cyanide sludge in the bottom. On the day of the accident the night shift leader began preparations to clean the remaining sludge by spraying 1 or 2 gallons of hydrochloric acid into the drying tank.After investigation it was concluded that the night shift leader unknowingly created hydrogen cyanide, a highly toxic compound, by combining sulphuric acid and zinc cyanide, two commonly used industrial chemicals. Hydrogen cyanide acts to block absorption of oxygen by the lungs and can cause death.After adding the sulphuric acid, the night shift leader, who worked alone and wore no respirator, climbed a ladder and descended into the tank. He did not test or ventilate the tank before entering. After several minutes, co-workers saw him struggling to climb out of the tank.Four other workers attempted to help and were quickly overcome. Two were forced back by the vapours. The other two collapsed, one inside the tank and the other with his head hanging over the edge. Fatality.
Lessons
Chemical safety.Ensure that good chemical safety practices are followed in the workplace:
1. Chemicals must be clearly labelled. Labels must be legible and in English. Warnings to be provided in other languages, as necessary.
2. More emphasis must be placed on dangers that can result from combining chemicals. Workers to be trained to recognise and anticipate hazardous chemical reactions.
3. Materials safety data sheets must provide necessary warnings as well as other important information on chemical hazards
Source :LOSS PREVENTION BULLETIN, 122, 9-10

May 10, 2020

Deblinding incident

A flash-back occurred as a blind was being removed from the outlet pass of a furnace, as it was being prepared for recommissioning after steam/air decoking.A crude preheat furnace was shutdown mid-run for decoking. On completion of the Steam-Air decoking procedure a maintenance fitter was deblinding prior to recommissioning.As a precaution, because hydrocarbons could be present, the fitter was instructed to wear a fresh air mask, which was supplied by an air line.Working from the burner platform, the fitter loosened the flange bolts (6" x 300 joint) with an accompanying whistle noise as the nitrogen pressure released from the flange joint. As the fitter lifted the blind (approximately half out) some liquid drained out (most likely condensate from the steam purge which was done when the blind was installed prior to the Steam-Air Decoking).There was an explosion, and a fire ball flashed across the burner platform from the central burners back to the loosened flange. The gas, escaping from the tower side of the blind, had entered the heater through the slots for the air register adjustment lever. The fitter left the platform, fortunately only receiving some singeing to his hair.The source of ignition was a pilot burner the potential hazard of ignition from this source was overlooked during the preparation for removal of the blind. The source of ignition may not have been a hazard had both sides of the blind been purged.
Source:ICHEME
LessonsThe accident investigation report recommended:
1. Positive isolation on both sides eg. at a double block and bleed. "Positive isolation" should be checked by opening the bleed, although care should still be exercised when breaking the flange in case the bleed is plugged, or
2. Positive isolation on one side and show of steam on the other. "Positive isolation" should be checked by carefully breaking of the flange to ensure that the valve is not passing, or
3. Show of steam on both sides

May 7, 2020

Gas leak at Viskhapatnam

Its very tragic to see the gas leak at LG polymers India Limited, today at Visak, with many people affected. The styrene gas leak reportedly occured from a storage tank. It pains me that we are continuing to have such incidents in the land of Bhopal. The Government did bring out a chemical safety and security rating system in 2013, but it died a natural death. See this article https://www.business-standard.com/content/b2b-chemicals/safety-rating-for-chemical-plants-a-step-in-right-direction-113102400722_1.htmlhttps://www.business-standard.com/content/b2b-chemicals/safety-rating-for-chemical-plants-a-step-in-right-direction-113102400722_1.html
This is what I has posted in my Linkedin account:
Will we ever learn from Bhopal?
It's really tragic to see scenes of people, including children, lying helplessly on the sides of the road in TV footage of the gas leak from LG polymers India Limited, Visakhapatnam. As I had mentioned in earlier posts, the late chair of the CSB, Carolyn Merritt asked me in 2004, the reason why PSM is not mandatory in India. I am still waiting for an answer. Even if PSM is made mandatory in India, the enforcing authorities lack the relevant competence to audit PSM systems. They are also highly understaffed. The ghosts of Bhopal are continuing to haunt us. In the recent COVID 19 deaths in Bhopal, a number of deaths were the victims of the gas leak in 1984, that had already weakened their health.

May 6, 2020

Be careful of unintended confined spaces

An accident involving 2 employees occurred in asbestos removal in an ethylene oxide unit. In order to remove the asbestos insulation around the system generator safely, the removal company was told to build a plastic tent with a lock round the steam generator.A form was drawn up for this purpose which stated that flanges and valves could not be built in the tent and 'without roof'. An oxygen test was carried out on the tent in four different places on man's height and each time, normal values were measured. Based on this, the foreman gave permission to continue working. Almost immediately of mounting the ladder in the tent, the two workers started to feel sick, became dizzy and everything turned black before their eyes. They managed to stumble outside and report the incident to the foreman.Within 10 minutes of the accident, the oxygen test by the operator was done again which gave normal values. The general foreman carried out another test with another meter and normal values were noticed again. Later inspection showed that the tent was built with a closed roof and a bypass line on the nitrogen line was built in the tent with two locked block valves. Several used spray cans of glue and other substances were found in the tent and it was stated on the cans that they should only be used in ventilation rooms.
The actual cause of the accident is unknown and although nitrogen leaks in the tent cannot be excluded, there is reason to assume that other gases may have caused the symptoms of the 2 workers of feeling sick, throat irritation and breathing difficulties.

Lessons
1. It is now required to enter the tent and carry out the job with two people.
2. In the specific case of tents around ethylene oxide reactors in which nitrogen leaks can never be excluded, the tent must be built with windows of translucent plastic on each wall and entering the tent and execution of works in the tent is exclusively reserved for people carrying fresh air masks.
3. A safety guard will watch the tent for the whole period of the activities equipped with air apparatus and a knife to cut open the tent if necessary. The guard must be trained in using compressed sir apparatuses. A guard must also be provided for each work level.
4. Oxygen tests must be carried out every two hours on different heights.
5. The use of spray cans of glue or polyurethane in closed tents is prohibited unless the roof is open.
6. Asbestos removal personnel will be formally re-instructed about the procedure and that the conditions on the form must be observed
Source:ICHEME

May 2, 2020

Drainage system explosion

An incident occurred when a manhole cover on an underground drainage system lifted. On investigation it was found that there was a high level in the drain sump, which was hot and steaming and local ground drains had back-flowed.The area was roped off and water lines put into the quench water outfall. This had an immediate cooling affect. Soon after the conditions of the drains were back to normal.The drains and downstream drains levels and temperatures were later checked and found to be normal.The report stated the following conclusions:The design of the oily drains system is such that a 100-200mm layer of hydrocarbons is always present in the sump drains. Hot water from the quench vessel vaporised light hydrocarbons in the drain system.The resultant overpressure pushed liquid back up the sumps, lifting the manhole covers.The water from the quench vessel was hotter that normal due to a dip in the raw water supply pressure.

Lessons
The report stated the following recommendations:1. Fit a pressure gauge to the quench vessel raw water supply to monitor fluctuations in supply pressure during reactor regeneration. Consider fitting a temperature alarm to the outfall.2. Check all vents on the gas separation drains system.3. Remove accumulated hydrocarbons from the gas separation drain sumps.4. Check drain sumps for solid debris and remove. Consider need to clean main drain runs at shutdown.
Source:ICHEME