On December 10, 2023, at 3:38 p.m., two explosions and a fire occurred in a polymer reactor at a facility in Mt. Vernon, Indiana. Property damage was estimated at $3.5 million.
Three months prior to the incident, on September 18, the company had shut down its polybutylene terephthalate resin unit for scheduled maintenance. On the day of the incident, the maintenance work was nearing completion, and operators were preparing the unit’s reactor system for startup. At 3:38 p.m., a heat exchanger exploded, ejecting several equipment fragments, including one that landed approximately 505 feet away near the facility’s boundary along the Ohio River. A second explosion and flash fire soon followed, rupturing a reactor.
The company's investigation concluded that the initial explosion in the heat exchanger was caused by the rapid, energetic decomposition of unstable organic peroxide that had formed and accumulated inside the equipment. The second explosion and flash fire, which destroyed the reactor, was caused by heat from the first explosion igniting flammable tetrahydrofuran vapor inside the reactor.
The exchanger and reactor were interconnected, with no isolation between the two pressure vessels. The design of the reactor’s outlet piping retained liquid in the piping. Because the piping could not fully drain, it contained polybutylene terephthalate polymer, butanediol, and tetrahydrofuran when the unit was shut down on September 18, 2023.
On December 10, operators began pre-startup activities. At 3:16 a.m., hot oil was sent through the tracing used to heat the reactor’s outlet piping. As the piping heated, the residual hydrocarbon material also heated, evolving tetrahydrofuran vapor that flowed into the reactor and the heat exchanger. A 3-inch nozzle on the heat exchanger remained open to ambient air, allowing oxygen into the reactor system. The tetrahydrofuran vapor reacted with available oxygen to form an organic peroxide compound. The organic peroxide continued to form for another 12 hours, until it exploded in a rapid decomposition reaction at 3:38 p.m. The heat from the explosion ignited additional flammable tetrahydrofuran inside the reactor, triggering the second explosion and a flash fire.
The company's investigation found that the company’s historical practice of leaving residual hydrocarbon material in the reactor’s outlet piping during shutdown created hazards that were neither recognized nor controlled. The reaction of tetrahydrofuran with oxygen produced the explosive organic peroxide. Before the incident, personnel had assumed that the cooled, solidified material could remain in the reactor’s outlet piping because it was not hazardous, creating a false sense of safety.
The investigation also found that a change to the reactor’s leak-testing procedure contributed to the incident. Previously, the reactor was leak-tested online under vacuum. The company switched to using pressurized nitrogen and moved the test into the maintenance outage. A management of change review had been approved to allow a leak test of the reactor during pre-startup activities. However, the review did not assess how the leak test might adversely affect those activities.
When the hot oil heated the reactor’s outlet piping, the procedure required adding nitrogen to the reactor system. However, the nitrogen flow was omitted due to the modified leak test. The company’s investigation concluded that the risk of performing simultaneous tasks during startup had not been evaluated.
Probable Cause
Based on the company's investigation, the CSB determined that the probable cause of the incident was heating the reactor’s outlet piping containing solidified polybutylene terephthalate polymer, butanediol, and tetrahydrofuran while a nozzle on an interconnected heat exchanger was open, allowing oxygen (air) to enter the equipment. These conditions generated tetrahydrofuran vapor, which reacted with oxygen to form an explosive organic peroxide, and also created a flammable atmosphere in the equipment, which then ignited and exploded after the organic peroxide energetically decomposed. The management of change review conducted for the reactor’s leak testing did not assess how the leak testing might affect the simultaneous pre-startup tasks, contributing to the incident. As a result, there was no nitrogen flow through the reactor system, allowing unstable peroxide to form and developing flammable conditions within the equipment.
Source: CSB.gov