June 24, 2022

WASTE WATER TANK INCIDENT

On September 9, 2003, Employees #1 and #2 were extending the guardrail system to the hatch and platform area on top of a tank located on the Brewery property. The tank was used for the storage of solid waste at the waste water treatment facility. The tank was 40 ft in height and 48 ft in diameter. The employees were arc welding the guardrail system, 40 ft above the ground, when an explosion occurred. Employee #1 fell to the ground receiving fatal injuries. Employee #2 fell to the inside of the tank, an opening of approximately 10 ft left due to the explosion. The tank had to be drained in order to recover the body. Employee #2 apparently died from injuries due to the explosion

Credit:Osha.gov

June 20, 2022

ARE YOU INSPECTING YOUR PILOT OPERATED VALVES CORRECTLY?

A Pilot operated relief valve failed to lift during planned recertification in the workshop. The cause of failure to lift identified as a plug fitted in the pilot exhaust port. Plug was removed from pilot exhaust port and RV functioned as intended.  On inspection of three remaining RV’s on compressor discharge, it was
found that another RV also had a plug fitted in the pilot exhaust port.

June 16, 2022

ARE YOU CONSIDERING HUMAN FACTORS DURING YOUR HAZARD IDENTIFICATION?

 An ammonia leak occurred in the machinery room of an unoccupied arena. An employee was attempting to add oil to an ammonia compressor when he observed a leak (fill hose was not attached). Approximately 200 lbs ammonia was released.
Qualified person was trained, but with minimal experience in this procedure. No written procedure was available, and an error occurred while executing the procedure. The shut-off valve type (wrench-operated,
mufti-turn, no position indicator) added complexities to the process.

Source: British Columbia Safety Authority 

June 12, 2022

WHY HAZOP STUDY IS IMPORTANT

 Approximately 200 lbs ammonia was released to atmosphere. The condenser safety valve activated due to ‘no cooling’ in the condenser while the ammonia compressor was operating. While restarting the plant after a power failure, the operator forgot to start the condenser circulating pump (which should be started before starting the compressor). The compressor was started without condenser cooling, and as a result, ammonia gas temperature began to rise, thus raising the gas pressure in the system. Eventually the gas pressure rose more than the safety valve setting, activating the safety valve which released the
ammonia to atmosphere.
The compressor’s high pressure safety cut off did not activate. The high pressure cut off is supposed to activate and shut off the compressor unit when the system senses a high pressure condition.

Source: British Columbia Safety Authority 

June 8, 2022

ARE YOU SPECIFYING PRESSURE GAUGES CORRECTLY?

 Approximately 100lbs ammonia was released into an unoccupied processing room of an industrial facility when a pressure gauge failed on the liquid line to an ammonia evaporator. Inspection revealed that a second pressure gauge (on the hot gas line for the same installation) was pinned at maximum pressure. Both pressure gauges had a range of 0 to 150psi and were installed in a system with an operating pressure of 150 to 160psi. The pressure gauge failed from over-pressure operation.

Source: British Columbia Safety Authority

June 4, 2022

ARE YOU INPECTING SMALL BORE TUBING?

 An ammonia leak occurred at a commercial-industrial facility. Approximately 10 lbs ammonia entrained in approximately 200 litres of compressor oil was released when a suction side 3/8-inch pressure sensing line failed. The suction side oil pressure pushed approximately 200 litres of oil from the reservoir onto the floor where the entrained ammonia then escaped to atmosphere. The 3/8-inch stainless steel tubing within the compression fitting failed when a circumferential crack completely fractured. The crack within the
3/8-inch stainless steel compression fitting did not show up on external inspection. Metal fatigue appeared to be a factor, along with unit vibration and initial metal stress within this type of compression joint.
 

The refrigeration contractor identified the main cause and factors leading to the failure as a severe vibration condition of the compressor. This severe vibration condition only occurs when only happens when the control slide valve is at, or at near its minimum position. The vibration was so intense that the contractor immediately shut the compressor down. Also, the contractor’s investigation discovered the ‘PHD’ vibration monitoring system was inactive. When the monitoring system was activated, the compressor in fact shut down on ‘high vibration.’ 

Source: British Columbia Safety Authority

May 31, 2022

ARE YOUR SAFETY DEVICES WORKING?

Ammonia was released at a recreational facility. A high pressure cut out switch failed to shut down a compressor when the compressor experienced a high pressure condition. Pressure continued to build until a safety relief device operated releasing ammonia gas to atmosphere via the relief stack,
which triggered the ammonia alarm.
The water supply line to the condenser had no protection and was subject to freezing during cold weather. The high limit switch was old (1986) and is mounted on the compressor base subjecting it to vibration. The safety relief operated as designed, venting gas to atmosphere, preventing a possible
catastrophic failure.
Source: British Columbia Safety Authority

May 27, 2022

SAFETY IN DESIGN OF PIPING

 https://www.hydrocarbonprocessing.com/magazine/2018/february-2018/environment-and-safety/safety-in-design-during-piping-engineering

 "A process engineer must complete the preliminary preparations of process flow diagrams, material and energy balances, piping and instrumentation diagrams (P&IDs), process control philosophy, and identification of the hazardous nature of raw materials, chemicals, byproducts and final products. Afterward, documents including process equipment layout drawings (plan and elevation) and unit plot plans are issued to engineers from other disciplines.

Involving engineers from different disciplines in the design phase provides unique perspectives that add value to basic documents, such as improved safety design features. Discipline engineers are required to consider design and safety requirements that are applicable for their specific domain as per local, national, international, industry-specific and company standards and regulations, and good engineering practices.

The role of a piping engineer during the design of piping systems is explored here, as well as how that piping engineer can—from the initial design phase—lower the risks that can arise from handling hazardous materials, contribute to reducing potential liability and help create a safer environment for the public".

READ THE FULL ARTICLE IN LINK


 

May 23, 2022

CONTROL HAZARDOUS ENERGY

 https://www.aiche.org/ccps/control-hazardous-energy-lock-out-and-tag-out

"Lock-out and tag-out (LOTO) is a critical part of a strong all-around safety program. In LOTO, maintenance employees work with production employees to positively prevent all forms of hazardous energy from causing harm. Hazardous energy comes in many forms. Electrical energy can cause electrocution and burns, provide ignition to flammable atmospheres, and activate mechanical equipment. Steam can cause burns or initiate hazardous reactions. Nitrogen can cause asphyxiation. Chemical flow can cause uncontrolled reaction and injury. When a piece of equipment is being worked on, all sources of hazardous energy must be securely and positively locked out until the equipment is operational. Untold numbers of major process safety incidents and individual injuries have been caused by failure of LOTO. A prime example is the Bhopal catastrophe, one of the worst incidents ever to have occurred, which was caused in part by the failure of LOTO. Recently, a company process safety manager called CCPS asking for help in persuading a newly acquired facility within his company to implement a LOTO program. The manager was frustrated because, as the plant director stated, “We understand completely that maintenance workers are endangered if power or material flow were allowed to equipment they are servicing. That’s why no one would ever activate a switch or valve during a maintenance activity. LOTO is just extra, unnecessary work.” The company process safety manager knew that with the plant director’s attitude, the plant could be on the road to disaster. Could CCPS help him make the case for LOTO? At CCPS, we firmly believe that it is better to learn from the mistakes of others rather than to learn by painful, personal experience. So we asked CCPS member companies to give us examples of accidents caused by LOTO failures, and to provide testimonials about the importance of LOTO. The purpose of this article is to share this information with you, to help you lead the implementation or improvement of LOTO in your
company. A brief overview of LOTO procedures and tools are provided, as are references to more detailed resources."

May 19, 2022

WHAT IS A BLEVE?

  http://www.hrdp-idrm.in/e5783/e17327/e27015/e27750/

For a BLEVE situation following four conditions must be present:-

  1. There must be a substance in liquid form. Most of the destructive BELEV's that have occurred have involved flammable liquids and liquefied flammable gases. BLEVE can occur with any liquid, even water. The only difference is that with non¬flammable liquids there is no fireball. However, there will still be damaging effect including the propagating of creaks in the structure of the container together with possibility of subsequent failure and propulsion.
  2. The liquid must be in a container like sphere, bullet, and road/rail tanker.
  3. The contained liquid must be at a temperature above its normal boiling point at atmospheric pressure at the time container allows the pressure inside to build up above atmospheric pressure, the fluid, in the container is able to remain in the liquid state, even through its temperature is above its normal boiling point. This increase in pressure raises the Boiling point of the contained liquid above its boiling point.
  4. There must be a failure of the container in order to have BLEVE. This container failure can be due to following courses:
  • Flame impingement.
  • Internal structural weakness of the container
  • Failure of improperly designed SRV
  • Impact from a mechanical cause such a road accident, tanker derailment allowing flammable liquid to flow out.

 

May 10, 2022

SAFE ACCESSING OF PRESSURE VESSELS

 https://www.kan.de/en/publications/kanbrief/industry-40-vision-or-reality/safe-accessing-of-pressure-vessels

"Operatives and technicians must frequently climb into pressure vessels in order to perform construction, maintenance, repair and inspection work. However, the access points through which they must pass for this purpose are often so small that although access is possible, rescuing these personnel in the event of an accident presents considerable difficulties. The Polytechnic University of Milan has conducted a number of studies into this issue in the course of two degree theses."

SEE THE LINK FOR FULL ARTICLE

May 6, 2022

NON METALLIC GASKETS - AVOIDING LEAKS AND BLOWOUTS

 https://www.plantengineering.com/articles/nonmetallic-gaskets-avoiding-leaks-and-blow-outs/

"The compressive stress on a gasket plays a larger role in its ability to maintain pressure than its tensile strength.
By Dave Burgess October 1, 1999

The compressive stress on a gasket plays a larger role in its ability to maintain pressure than its tensile strength. Why is this significant? It is the reason for many gasketed joint problems!

In a classic scenario, a joint is assembled without controlled bolt loads; that is, without known and controlled bolt torques. The joint withstands a hydro test at 1.5 or 2 times rated pressure, yet leaks or blows out after a period of service at pressures well below the test pressure.

Was this failure due to a loss of gasket tensile strength? Probably not. Gasket tensile strength alone cannot be counted on to hold system pressures. What very likely occurred was loss of compressive stress on the gasket."

READ THE COMPLETE ARTICLE IN THE LINK


May 2, 2022

ETHYLENE OXIDE RELEASE INCIDENT

 https://dnrec.alpha.delaware.gov/croda-questions-answers/

 "What happened at the Croda Atlas Point plant?

At 4:15 p.m., Sunday, November 25, 2018 ethylene oxide (EO) was accidentally released into the air from Croda’s ethylene oxide plant. Since EO is very soluble in water, Croda deployed its water deluge system to contain as much of the release as possible. Croda personnel also began transferring the EO from the leaking vessel in the processing equipment to a secure containment vessel. Local responders and DNREC Emergency Response arrived. Water suppression continued. With input from Croda personnel, responders determined that by opening two nitrogen valves in the processing equipment, the remaining EO from the leaking vessel could be transferred to the non-leaking vessel, stopping the release."

 READ THE LINK FOR COMPLETE DETAILS...

 

 

 

 

 


 

 

April 29, 2022

SODIUM CYANIDE LEAK

 Incident
A plant operator responded to a bund alarm and observed sodium cyanide solution overflowing from a storage tank. A pool of approximately 84 000 litres of solution had formed and was contained within the tank bund. The site emergency plan was enacted and an exclusion zone was established around the area whilst the product in the bund was transferred to another tank. The concrete bund contained the spill, and the recovered solution and all of the washings were kept for use in future blending operations.

Cause
The combination of a faulty valve and failure by an operator to follow standard operating procedure, led to the tank overfilling. The overflow spilt into the bunded area and activated the bund alarm.

Consequences
The defective valve was repaired and the tank high-level critical alarm system has been reviewed and improved. The tank overflow piping is also under review to identify options to prevent recurrence. The responsible operator has been counselled on appropriate self-check work systems. There were no injuries or damage to any property as a result of the incident and the emergency response plan functioned as intended.

Source: Department of Minerals and Energy, Australia

April 25, 2022

CHLORINE LEAK DUE TO STRESS CORROSION CRACKING OF SS BOLTS

 Incident
Approximately 150 kg of chlorine gas was released over a period of 140 minutes, due to failure of bolts on a vacuum gas regulator attached to an on-line liquefied chlorine gas drum, used for water treatment. The incident occurred outside work hours, however plant operators were not called out, as the plant alarm system was not correctly programmed. Impact from the release to the surrounding community was limited to chlorine odour being detected by a passing motorist who reported the odour to the operator of the
site. The leak was isolated by a plant operator who arrived at the scene after the release was reported.
Cause
Inspection of the vacuum gas regulator revealed that the release was due to the failure of four bolts on the regulator. Material test results show that the failure of the stainless steel bolts was due to chloride-induced-stress cracking from chlorine attack, which is assumed to have resulted from an extremely small leak over a short duration.
Consequences
As part of the investigation, a number of changes to prevent recurrence of the event have been identified and implemented. These include introduction of a weekly leak check, the company committing to inspection of all vacuum regulators, the replacement of any inappropriate bolts and reprogramming of the chlorine alarm. In addition, the company will investigate the use of different alloy bolts.

Source: Department of Minerals and Energy, Australia 

April 21, 2022

NITROGEN HOSE BURST AND RELEASED AMMONIA

Incident
A release of ammonia occurred from a chemical plant when a hose burst following maintenance to an ammonia filter. The release of ammonia was detected by operators due to ammonia alarms and a high flow of ammonia to the plant. The site emergency siren was activated to alert people of the incident and operators isolated the supply of ammonia to the plant. Operators donned personal protective equipment
and doused the leak with water in order to gain access to the area to isolate the leak.
Cause
Ammonia filters were used to remove contaminants from the liquid ammonia, prior to it being processed in the plant. An essential step in the maintenance of filters is a nitrogen purge of the system. After purging occurs, the filter is changed, resealed and the nitrogen hose disconnected. The relevant valves are then opened to recommission the system with ammonia. In this instance, the nitrogen hose remained connected to the filter and drain valves were left open allowing the hose to become
pressurised with liquid ammonia. While the hose was suitable for the pressures normally experienced under service with nitrogen, the hose was not suitable for the much higher pressures of liquid ammonia and as a result the hose burst in two places.
Consequences
The incident occurred as a result of the failure to follow the appropriate procedure and the company has taken the action of reviewing the competence of each operator to carry out the task. The company has also reviewed the operating procedures associated with the filter cleaning process to ensure they are appropriate. 

Source: Department of Minerals and Energy, Australia

April 17, 2022

RELEASE OF TOXIC LIQUID THROUGH STEAM COIL LINE GASKET LEAK

 Incident
A release of toxic liquid (containing arsenic trioxide) from a storage tank occurred following the shutdown of a chemical plant. The release occurred from a steam coil passing through a storage tank used to store the solution during the shutdown. The release flowed into a surface-drainage system,through a series of secondary catchment sumps and ponds, into Cockburn Sound.
Cause
An investigation into the incident has identified that the toxic liquid was released through a hole in a gasket of a flange. The flange was located on the steam coil pipework within the tank. It was found that the steam-line terminated outside the bunded area in a partially-covered surface-drainage system.
Consequences
To prevent a recurrence, all steam-lines within the plant were cut to ensure that they terminated within the bunded area. The company has also decommissioned the plant and will commission a new plant that does not utilise arsenic compounds.

Source: Department of Minerals and Energy, Australia 

April 13, 2022

FAILED GASKET DURING START UP

 Incident
A mixture of process gases was released to the atmosphere through a failed gasket during the start-up of a chemical plant. Operators had just completed the start-up when they heard a large steam release and received alarms from ammonia detectors. The plant was shutdown, however the plume released travelled off-site necessitating the evacuation into refuges of a small number of workers on a neighbouring site. None was injured as a result of the release.
 

Cause
An investigation showed that the gasket failed as a result of a hole in a boiler tube which had allowed water to pass from the boiler side into the process side. The temperature generated during start-up caused the pooled water to rapidly boil leading to a surge in pressure which resulted in the failure of the gasket. Non-destructive testing of the boiler tubes showed gouge-type corrosion believed to have been caused by flow distribution problems in the boiler. This resulted in excessive metal temperature, which led to corrosion of the tube. 

Consequences
A complete boiler inspection has now been conducted and boiler tubes showing signs of corrosion have been plugged off. Actions to prevent a recurrence include the addition of insulation at the top of all boiler tubes and further investigation into the boiler water chemistry to minimise potential for corrosion. The company has also modified the boiler to incorporate a drain valve in order to provide early warning in the event of water leakage.

 Source: Department of Minerals and Energy, Australia

April 9, 2022

START UP INCIDENT IN AMMONIA PLANT

 Incident
A mixture of synthesis gas and ammonia was released from an ammonia plant during the start-up process following a shutdown for maintenance. The release occurred from a high vent after ammonia had been allowed to collect in the vent system through a valve left open as a result of failure to tag the valve as out of service.
During the start-up, operators failed to control levels in the process, resulting in a high level alarm in an ammonia catchpot which led to a release of synthesis gas (as designed) into the vent system. However, as the vent system already contained ammonia, the gas mixture was forced out of the high vent. The wind direction took the gas cloud over an adjacent construction area on the same site resulting in fourteen
contract employees experiencing irritation and discomfort and later seeking medical attention. Six of these contractors were physically affected as a result of the exposure but nobody suffered serious or long-term injuries. The ammonia release dispersed and was not detected at neighbouring premises.
Cause
The incident was caused by a combination of factors including a failure of the tagging system and the failure to adequately control the catchpot level during start-up.
Consequences
The tagging system for equipment which is out of service, has been reviewed to ensure during maintenance there is no unauthorised operation of equipment. Resource allocation has been reviewed to ensure that process control is secured and level indicators in the catchpot have been assessed to ensure accuracy for process control. Also, workers at the adjacent construction site will now carry gas respirators at all times and will be notified of any operating conditions, such as start-ups and shutdowns, with the potential to lead to releases of gas.

Source: Department of Minerals and Energy, Australia