Incident
A mixture of process gases was released to the atmosphere through a failed gasket during the start-up of a chemical plant. Operators had just completed the start-up when they heard a large steam release and received alarms from ammonia detectors. The plant was shutdown, however the plume released travelled off-site necessitating the evacuation into refuges of a small number of workers on a neighbouring site. None was injured as a result of the release.
Cause
An investigation showed that the gasket failed as a result of a hole in a boiler tube which had allowed water to pass from the boiler side into the process side. The temperature generated during start-up caused the pooled water to rapidly boil leading to a surge in pressure which resulted in the failure of the gasket. Non-destructive testing of the boiler tubes showed gouge-type corrosion believed to have been caused by flow distribution problems in the boiler. This resulted in excessive metal temperature, which led to corrosion of the tube.
Consequences
A complete boiler inspection has now been conducted and boiler tubes showing signs of corrosion have been plugged off. Actions to prevent a recurrence include the addition of insulation at the top of all boiler tubes and further investigation into the boiler water chemistry to minimise potential for corrosion. The company has also modified the boiler to incorporate a drain valve in order to provide early warning in the event of water leakage.
Source: Department of Minerals and Energy, Australia
No comments:
Post a Comment