December 13, 2010

Major Fire at Pharma Plant

Thanks to Abhay Gujar for sending information about a major fire at a Pharma plant in Punjab. Three people including a General manager and chemist have reportedly died. Did a blast in a reactor cause it? One of the articles mentions that a reactor burst due to "oversteaming".
Unfortunately, such accidents keep occurring in India and other countries also. Batch reactors must be treated with great respect. A solid looking reactor will destroy itself to pieces if it is overpressurised beyond its design limits due to maloperation.
Read the articles in these links:
Link 1
Link 2


December 11, 2010

Plant explosion kills two - pay heed to your process near misses and incidents

A news article mentions that two workers were killed and two others were seriously injured in an explosion and fire at a West Virginia chemical plant on Thursday afternoon. The explosion occurred at a plant that reprocesses highly flammable potassium titanium fluoride salts, zirconium, and other chemicals for use in the aluminum industry. The article mentions that "It is the fourth fire in the last five years and the second fatal fire since 2006. The AL Solutions plant has been the site of multiple fires since it opened in 1991, then under Jamegy Inc. In 1995, a propane tank exploded, killing one worker and injuring another. Another fire broke out in 1997. On July 18, 2006, a worker was killed when a similar explosion and fire ripped through the foundry of the facility. On December 21, 2006, another blaze broke out after a forklift malfunctioned, setting ablaze a tank filled with titanium. On August 2, 2009, yet another fire erupted as employees were shoveling zirconium into barrels".
Pay heed to your previous incidents and learn lessons from them. Even if you have excellent management systems for process safety, there is no use if the your organisation does not incorporate the learning's of past incidents in its DNA.
Read the article in this link.

Potassium cyanide incident

An incident has occurred where about 200 L of potassium cyanide has leaked into a vessel containing acids which has liberated the highly toxic hydrogen cyanide gas. Many pesticide manufacturing companies also use cyanide for their process and the handling and storage should be done with great care. I had observed a case where rainwater had entered a strongroom storing cyanide and reacted with it. The rain water entered the locked room through a drain which was open to the outside. Manage your toxic chemicals safely or they will manage you. Read the full article in this link.

December 10, 2010

7 injured in pesticide plant explosion

A news article mentions about an explosion in a pesticide plant in China. It appears to be an explosion in a solvent storage tank. Storage tanks are often not given the importance they deserve. For one thing, they are located away from the plant and the further away from the plant, the more likely it is going to receive less attention. It is a good practice to conduct surprise audits of your storage locations to check any deviations from the safety systems provided.
Read the article ( it has got pictures in page 2 and 3 also) in this link.

December 9, 2010

Did inferior raw materials cause the cordite factory blast?

A newspaper article reports that insiders of the Cordite factory believe that supply of poor quality material could be to blame for the blast that killed 5 workers on November 25. I have observed that the trend in the industry is to go for the lowest cost (L1). While process safety does not prohibit you from going for the least cost supplier, ensure that you do not create process safety problems due to inferior quality. Read the article in this link.

December 8, 2010

Chemical Terrorism and mock drills

The department of homeland security in the US has recently conducted a mock drill for a terror attack induced scenario. The scenario was three simultaneous accidents - ammonia leak from rail tanker, sulphuric acid leak from rail tankers and a train derailment with chlorine tankers.
In India, though we do have a Chemical Accidents (emergency planning, preparedness and response) rules, 1996, we have a long way to go before we are truly prepared for what the US is already prepared.
Read the article about the mock drill in this link.

December 7, 2010

Radioactive sources and process safety

Some instruments use radioactive sources for their functioning. Also, radioactive sources are maintained by large chemical companies who use them for radiography of welds etc. Maintain the radioactive source as per the conditions required by law. In a recent incident, an oil company was fined 300,000 pounds after exposing workers to radiation. The article mentions the following:

"The incident happened while Schlumberger was contracted to undertake wireline logging operations as part of the Maersk drilling programme for the Cawdor oil well. During the process a logging tool fitted with a radioactive source was supposed to be lowered into the well, the court heard. But the lowering process failed and the radioactive source lay on the drill floor for about four hours before being found, during which time 14 workers were exposed to radiation. The Health and Safety Executive said it was "only by good fortune" that the mistake had been discovered before it had more serious consequences"."Had someone held it, even just for a few minutes, they would have received a significant radiation dose which may have resulted in injuries to their hands and increased their risk of developing cancer in later life."

Read the article in this link.

December 6, 2010

Diving to disaster - lessons from the Air India incident


O   On 26.5.10, Air India express flight (Boeing 737-800 NG aircraft) from Dubai to Pune, when on normal flight, suddenly plunged from 37000 feet to 30200 feet. The commander of the flight had over 6000 hours of flying with 870 hours on similar type of aircraft while the copilot had total of 1310 hours with 968 hours on similar type of aircraft. The commander was 39 years old and the copilot was 26 years old. The commander went out of the cockpit to the washroom after the plane was on autopilot. He was only out for a few seconds when the plane started diving down. The copilot was not responding to open the cockpit door. Finally the commander opened the door with an emergency access code and entered. The flight was then stabilised and landed safely later. The reasons for the incident was that the copilot, while adjusting his seat, inadvertently pushed the control column, resulting in the plane diving down. He then reportedly panicked and could not open the cockpit door for the commander to enter. The investigation report has great parallels to process safety. On reading the report the following facts emerge:
  1. The commander when asked why he left the cockpit to the washroom without asking the cabin steward to be in the cockpit (as is standard practice in the aviation industry – not to leave any pilot alone in the cockpit) reported that it was not in the SOP.
  2. The co pilot has reportedly told investigators that he panicked when the dive occurred and the overspeed alarm was blaring.
  3. The simulator training given to qualify the pilots does not include the scenario of autopilot engaged and control column pushed inadvertently.
  4. The position of chief of training for Air India has been lying vacant since June 2008.
Lessons to be learnt:
  1. Make sure your SOP’s are current
  2. The age of the copilot was 26 years old. He panicked when the situation occurred as he was not trained to handle the situation.Make sure your control room operators are properly trained in all scenarios. Use simulator training to educate them
  3. Make sure critical positions like process safety, training and HR (other than operations) are filled up with competent personnel.
Read the full report in this link. Kudos to the DGCA for putting the report up on their website!! The transparency of the government may, I hope, slowly result in the formation of an investigating agency like the CSB for investigating chemical incidents in India!

December 5, 2010

Beware of that spark!

Electrical hazardous area classification is often a confusing item for plant personnel. They are more familiar with pressures, temperatures and the like. But basic understanding of the different terminologies should be understood. An article mentions the following:
"Installing electrical and automation panels in hazardous areas requires use of one of three protection methods: explosion-proofing (EXD), purge and pressurization (EXP) or intrinsic safety (IS).
EXD contains the pressure of the explosion, and then cools it through a critical flame path to a level that will not ignite the surrounding environment.
EXP protects the environment by segregating hazardous material from the ignition source before equipment is powered. First, explosive mixtures are purged from the enclosure; then a positive pressure is maintained inside the enclosure to insure hazardous gasses do not propagate back in during operation.
IS protection limits the energy entering the hazardous area to a level incapable of igniting the easiest ignitable concentrations of gas/air mixtures under fault conditions".

Read more of the article in this link.


December 4, 2010

Incident at DuPont plant hospitalises two

An article mentions that two workers were exposed to monomethyl amine which was released from a railcar sample line while taking sample.
Read the full article in this link

Fire in a chlor alkali plant and citations from OSHA

A blast in a chlor alkali plant in China has been reported to have killed three people. Resons are being investigated. Read the article in this link.
In another development, OSHA has cited Huntsman Petrochemical of Houston Texas of violations in PSM. The article is quoted below:
"OSHA began its investigation June 7 in response to an incident in one of the company’s process units.Alleged serious violations include failing to incorporate operating procedures for all safety devices in the company’s operating guide; adequately train employees in safe operating procedures; properly shut down process equipment; identify and isolate all energy sources to the equipment; and to ensure lockout/tagout energy isolating devices such as line valves prior to employees performing maintenance on the equipment. A serious citation is issued when there is a substantial probability that death or serious physical harm could result from a hazard about which the employer knew or should have known. The company has 15 business days from receipt of the citations to comply, request an informal conference with OSHA’s area director in Houston, or contest the citations and penalties before the independent Occupational Safety and Health Review Commission".

Read the article in this link.

December 3, 2010

Fire in natural gas furnace in ammonia plant

A news report mentions a in a furnace in an ammonia plant due to rupture of a natural gas pipeline.
When I was shift in charge in an ammonia plant 30 years ago, we used to light up the start up heater for heating up the ammonia convertor. This furnace was a natural draft and naphtha fuel fired design. We used to keep increasing the firing while closely monitoring the rate of heating up. The pressure in the gas coil was 220 Kg/cm2. The burner flames used to be coming out of the top of the stack during the final phases of heating. Luckily we never had any incident of coil rupture in this heater or otherwise I would not be here today!!
Furnace can Kill if you mistreat them. Read your operating instructions, have your protection systems maintained and conduct periodic inspection of the coils.
Read the article in this link.

Axial misalignment causes a fatigue failure -Quantas A380 incident

The ATSB which is conducting investigations into the engine failure incident that occurred to the Airbus A 380 aircraft on November 2010, has mentioned the following in a safety alert:"A subsequent examination of the aircraft indicated that the No 2 engine had sustained an uncontained failure of the Intermediate Pressure (IP) turbine disc. Sections of the liberated disc had penetrated the left wing and the left wing-to-fuselage fairing, resulting in structural and systems damage to the aircraft. The No 2 engine was removed from the aircraft and disassembled in an authorised engine workshop for examination, under the supervision of the Australian Transport Safety Bureau. In addition, a large section of liberated IP turbine disc was also recovered from Batam Island for examination. Those examinations are ongoing. Recent examination of components removed from the failed engine at the Rolls-Royce plc facility in Derby, United Kingdom, has identified the presence of fatigue cracking within a stub pipe that feeds oil into the High Pressure (HP) / Intermediate Pressure (IP) bearing structure. While the analysis of the engine failure is ongoing, it has been identified that the leakage of oil into the HP/IP bearing structure buffer space (and a subsequent oil fire within that area) was central to the engine failure and IP turbine disc liberation event.

Further examination of the cracked area has identified the axial misalignment of an area of counter‑boring within the inner diameter of the stub pipe; the misalignment having produced a localised thinning of the pipe wall on one side.

Misaligned stub pipe counter-boring is understood to be related to the manufacturing process. This condition could lead to an elevated risk of fatigue crack initiation and growth, oil leakage and potential catastrophic engine failure from a resulting oil fire".

Read the full report in this link. Those of you who are responsible for asset integrity in chemical plants - please note that it only requires a small error to cause a big disaster.

The lessons from Bhopal – Relevant more so today

26 years ago, on the night on December 2nd/3rd, 1984, on a wintry night in Bhopal, thousands of men, women and children died an excruciating death when MIC leaked from the Union Carbide factory. The survivors and the next generation children born to those exposed to the gas still are suffering from the effects of the gas. Bhopal is an ongoing tragedy and should never be forgotten. The lessons from the Bhopal Disaster are very relevant even after 26 years:
1. Do not cut costs without looking at the effects on process safety
2. Maintain all your layers of defense.
3. Continually ensure that competency of personnel operating and maintaining plants are updated and current
4. Be prepared for the worst case scenario.
5. Understand the risks and measures to eliminate / reduce or control them
6. Learn from your past incidents. Those who do not learn are condemned to repeat the incidents.
7. Pay heed to your process safety management system audit reports
Read my older post comparing the Bhopal and the BP incident of 2005 in this link

December 1, 2010

Maintain your mitigation systems - they are your last lines of defense

A news report mentions that a hydrofluoric acid leak in a plant has been effectively contained by the plants mitigation systems, which worked as they were intended to do. Many of operating personnel (myself once included!) do not give enough importance to mitigation systems thinking that they will never be needed. Mitigation systems (dyke walls water sprays, interceptor dykes etc) are not required normally but are very useful in low frequency high potential incidents. In the said incident the article mentions that the company says that they haven't had a leak like this in "years and years".
Read the article in this link

November 30, 2010

Human issues in the Deepwater Horizon blowout

An Interim Report on causes of the Deepwater Horizon oil rig blowout and ways to prevent such events by the committee for the analysis of causes of the Deepwater Horizon explosion, fire, and oil spill by the National Academy of Engineering; National Research Council mentions the following:
"1.The incident at the Macondo well and Deepwater Horizon MODU was precipitated by the decision to proceed to temporary abandonment of the exploratory well despite indications from several repeated tests of well integrity [the test type known as a negative (pressure) test] that the cementing processes following the installation of a long-string production casing failed to provide an effective barrier to hydrocarbon flow (Sections II and III).
2. The impact of the decision to proceed to temporary abandonment was compounded by delays in recognizing that hydrocarbons were flowing into the well and riser and by a failure to take timely and aggressive well-control actions. Furthermore, failures and/or limitations of the BOP, when it was actuated, inhibited its effectiveness in controlling the well (Sections III and IV).
3. The failures and missed indications of hazard were not isolated events during the preparation of the Macondo well for temporary abandonment. Numerous decisions to proceed toward abandonment despite indications of hazard, such as the results of repeated negative-pressure tests, suggest an insufficient consideration of risk and a lack of operating discipline. The decisions also raise questions about the adequacy of operating knowledge on the part of key personnel. The net effect of these decisions was to reduce the available margins of safety that take into account complexities of the hydrocarbon reservoirs and well geology discovered through drilling and the subsequent changes in the execution of the well plan (Section VI).
4. Other decisions noted by the committee that may have contributed to the Macondo well accident are as follows:
• Changing key supervisory personnel on the Deepwater Horizon MODU just prior to critical temporary abandonment procedures (Section VI);
• Attempting to cement the multiple hydrocarbon and brine zones encountered in the deepest part of the well in a single operational step, despite the fact that these zones had markedly different fluid pressures (because of the different fluid pressures, there was only a small difference between the cement density needed to prevent inflow into the well from the high-pressure formations and the cement density at which an undesirable hydraulic fracture might be created in a low pressure zone) (Section II);
• Choosing to use a long-string production casing in a deep, high-pressure well with multiple hydrocarbon zones instead of using a cement liner over the uncased section of the well (Section II);
• Deciding that only six centralizers would be needed to maintain an adequate annulus for cementing between the casing and the formation rock, even though modeling results suggested that many more centralizers would have been needed (Section II);
• Limiting bottoms-up circulation of drilling mud prior to cementing, which increased the possibility of cement contamination by debris in the well (Section II);
• Not running a bond log after cementing to assess cement integrity in the well, despite the anomalous results of repeated negative-pressure tests (Section II);
• Not incorporating a float shoe at the bottom of the casing as an additional barrier
to hydrocarbon flow (Section II); and
• Proceeding with removal of drilling mud from the well without installing the
lockdown sleeve on the production casing wellhead seals to ensure the seals could not be shifted by pressure buildup under the seals (Section II).
5. Available evidence suggests there were insufficient checks and balances for decisions involving both the schedule to complete well abandonment procedures and considerations for well safety (Section VI).
6. The decisions mentioned above were not identified or corrected by the operating management processes and procedures of BP or those of their contractors or by the oversight processes employed by the Minerals Management Service (MMS) or other regulators (Sections VI and VII).
7. Currently, there are conflicting views among experts familiar with the incident regarding the type and volume of cement used to prepare the well for abandonment.There are also conflicting views on the adequacy of the time provided for the cement to cure. These factors could have had a material impact on the integrity of the well (Section II).
8. The BOP did not control—or recapture control of—the well once it was realized that hydrocarbons were flowing into the well. Also, both the emergency disconnect system designed to separate the lower marine riser from the rest of the BOP and automatic sequencers controlling the shear ram and disconnect failed to operate (Section IV).
9. Given the large quantity of gas released onto the MODU and the limited wind conditions, ignition was most likely. However, the committee will be looking into reports (such as testimony provided at the MBI hearings) that various alarms and safety systems on the Deepwater Horizon MODU failed to operate as intended, potentially affecting the time available for personnel to evacuate (Section V).
10. The various failures mentioned in this report indicate the lack of a suitable approach for anticipating and managing the inherent risks, uncertainties, and dangers associated with deepwater drilling operations and a failure to learn from previous near misses(Section VI).
11. Of particular concern is an apparent lack of a systems approach that would integrate the multiplicity of factors potentially affecting the safety of the well, monitor the overall margins of safety, and assess the various decisions from perspectives of well integrity and safety. The “safety case” strategy required for drilling operations in the North Sea and elsewhere is one example of such a systems approach (Section VII)
Read the full report in this link.

November 28, 2010

Static electricity and explosives

An article in the Times of India mentions the following about the recent blast in the cordite factory at Ooty:"factory staff suggest that mere "human vibrations" are enough to trigger a calamity in the highly explosive environment of the dough making unit....At the 13 by 13 feet at the incorporation unit where the blast occurred, earth plates and poles have been positioned for the workers to release their "vibrations" after they perform every small task."
Apparently the "human vibrations" they are talking about is nothing but static electricity. A static discharge spark can readily detonate primary explosives. From the article, all measures to avoid static electricity generation were reportedly taken. It will be good if the investigation team shares reasons on what caused the accident without breaching confidentiality as it is a defense unit.
Read the Times of India article in this link.

Safety Integrity Levels - Hip or Hype?

Yesterday I attended a seminar on "Safety Integrity - Life cycle approach", organised by ISA at IIT, Madras.The IEC 61508 and 61511 standards were discussed. Having interacted with many users, I think the problem with the safety integrity approach lies somewhere between hip and hype. When I mean hip, many users think that just be implementing a SIL 3 capable system, everything will be hunky dory. Not so! It requires a lot of operations and maintenance inputs throughout the life cycle of the system to ensure that it maintains its reliability. While instrument manufacturers often tend to go overboard to sell their ides to the client and engineering, procurement and construction companies also tend to recommend such systems to their clients, ultimately it is the the client who has to decide what level of risk is he prepared to take and whether existing instruments will be sufficient, without going in for a detailed SIL study. Unfortunately many clients do not have the technical support requires to make such decisions and rely on the designer. I go back to the analogy I had given in my earlier posts - We had operated a pneumatic controlled ammonia plant (no DCS, no smart transmitters, no fieldbus, no HART) quite successfully in the eighties for over a decade without an instrument failure that caused a spurious trip or fail dangerous undetected state. The answer to the question whether safety integrity is Hip or Hype lies in the understanding of risks by the client and is solely based on his decision. So the answer lies inbetween!!

November 26, 2010

Blast in cordite factory

Its ironical that my last blog was about a blast in a test tube. Today there is news about a massive explosion in the cordite factory in Ooty, that killed at least 5 people.A news report mentions that "An intermediary process of mixing dough (a nitrocellulose-nitroglycerine paste) was in progress when the explosion occurred. It brought down a part of the building".
Read the articles in these links":
Blast1
Blast2

November 25, 2010

A test tube explosion!

An accident at a school lab in the US indicates the dangers of chemicals. A news article mentions the following: "It was a simple science experiment designed to create a small combustion in a glass container and teach high schoolers about chemical reactions.A mixture of three chemicals -- potassium chlorate, manganese dioxide and glycerin -- and a dash of sugar heated over a Bunsen burner in a test tube were supposed to cause a pop and a puff of smoke, demonstrating an exothermic reaction to a class of Grade 11 students at F.J. Brennan Catholic high school.But something went wrong Tuesday morning. The test tube exploded, launching shards of glass across the science lab and injuring teacher Steve Pellarin and three students.No one was seriously hurt, but Pellarin sustained cuts to his face and hands. The students had minor lacerations, and no one sustained any chemical burns, said Windsor-Essex Catholic District School Board spokeswoman Jill Braido".
Read the article in this link.
Wikepedia mentions the following:
"Potassium chlorate is often used in high school and college laboratories to generate oxygen gas[citation needed]; it is a far cheaper source than a pressurized or cryogenic oxygen tank. Potassium chlorate will readily decompose if heated in contact with a catalyst, typically manganese (IV) dioxide (MnO2). Thus, it may be simply placed in a test tube and heated over a burner. If the test tube is equipped with a one-holed stopper and hose, warm oxygen can be drawn off. The reaction is as follows:
2KClO3(s) + heat → 3O2(g) + 2KCl(s)
The safe performance of this reaction requires very pure reagents and careful temperature control. Molten potassium chlorate is an extremely powerful oxidizer and will spontaneously react with many common materials. Explosions have resulted from liquid chlorates spattering into the latex or PVC tubes of oxygen generators, as well as from contact between chlorates and hydrocarbon sealing greases. Impurities in potassium chlorate itself can also cause problems. When working with a new batch of potassium chlorate, it is advisable to take a small sample (~ 1 gram) and heat it strongly on an open glass plate. Contamination may cause this small quantity to explode, indicating that the chlorate should be discarded".
For folks operating chemical reactors in the industry, know what you are dealing with!