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June 23, 2020

Improper isolation incident

Part of a benzene plant was shutdown, as part of the annual shutdown programme. As part of the preparations for maintenance the main process sections were drained, purged and steamed in accordance with the set procedures. Work then began on the stripper column reboiler circuit, including two heat exchangers. The actions required for the preparation of one of the exchangers had been highlighted, and so it was assumed these actions had been completed. Under a Permit to Work the foreman and 4 of his team commenced on unbolting the exchanger end plate and the main channel end flange.
The work was not completed and was carried forward to the next shift. During the work it was noticed that the exchanger surface was still hot. This was assumed to be due to steaming operations in the shell side of the exchanger. The following day under a re-signed Permit to Work, the team continued with unbolting and the exchanger end plate seal was released. Hot condensate spilled out of the bottom section of the exchanger end channel. When the flow ceased the final bolts
were removed from the end plate flange and the end plate cover was rigged ready for lifting down to ground level. Approximately 10 minutes after the end plate was removed, a fitter working adjacent to the area was hit by a large flow of hot condensate, which flowed from the exchanger, impinged on a tube baffle plate and then sprayed over the fitter. He crawled away and colleagues put him under a safety shower until the ambulance arrived. The fitter received scalds to his back and neck. Investigations showed that there had been ineffective isolation of the exchanger system from the live LP plant steam supply. There was also passing valves on the condensate system which contributed to the presence of hot condensate. The highlighted had not in fact been completed and
there had been inadequate physical checking of the isolation work prior to handover for maintenance. The Permit to Work system had not highlighted potential hazards, and due to work overload was not being operated effectively.
Lessons
The following recommendations were made:
1. Key isolation valves should be checked for passing.
2. All work packs were re-checked for proper system isolation before shutdown work recommenced.
3. The organisation and supervision for the shutdown were reviewed and clear requirements for detailed recording and handover of progress between shift
teams were set.
4. A schedule was to be set up for a management review of the progress of the new coordination routine and for general safety auditing of the shutdown
activities on the plant.
5. The lessons learnt from the incident were to be circulated to other plants undergoing shutdown, to identify Best Practice for the future.
6. Generic recommendations from other condensate related incidents were to be reinforced.
Source:IChemE

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